Mainship 34 MK3 1983, "IBIS" with Perkins 200 Turbo.
Question: Multipart - Did I damage my Turbo or motor?
1) Could not get motor to shut down - kill buttons didn't work so tried shorting leads on back of switch. So in desperation I placed a plastic bag in front of air intake thus blocking the air input for maybe 5 -10 seconds. Motor kept going but very rough (and I'm told white smokey). When plastic was removed the engine resumed normal operation but there was some motor oil dripping/running out of the funnel shaped intake. Motor resumed normal operation. Checked later, there was no noticeable crank case oil loss.
Would be interested in y'all's thoughts.
2)Now, "The Rest of the Story" as Paul Harvey used to say
Since depriving air didn't work, I shut down fuel supply. It idled awhile then quickly started to race so high to a scream - I bailed out - was afraid it would blow. It made no big noise and just coasted to a stop
Current status: I repaired the shutdown solonoid wire connection, and found the shutdown linkage. A quick turn of the key to check if seized and it started without bleeding (sounded normal) - shutdown button worked. Bleeding fuel line is next
Question: Multipart - Did I damage my Turbo or motor?
1) Could not get motor to shut down - kill buttons didn't work so tried shorting leads on back of switch. So in desperation I placed a plastic bag in front of air intake thus blocking the air input for maybe 5 -10 seconds. Motor kept going but very rough (and I'm told white smokey). When plastic was removed the engine resumed normal operation but there was some motor oil dripping/running out of the funnel shaped intake. Motor resumed normal operation. Checked later, there was no noticeable crank case oil loss.
Would be interested in y'all's thoughts.
2)Now, "The Rest of the Story" as Paul Harvey used to say
Since depriving air didn't work, I shut down fuel supply. It idled awhile then quickly started to race so high to a scream - I bailed out - was afraid it would blow. It made no big noise and just coasted to a stop
Current status: I repaired the shutdown solonoid wire connection, and found the shutdown linkage. A quick turn of the key to check if seized and it started without bleeding (sounded normal) - shutdown button worked. Bleeding fuel line is next