Dougcole
Guru
Three weeks after I finished replacing my port tank, my starboard tank started leaking. Gut punch.
Not sure how many of you followed my thread from April about replacing the leaking port side fuel tank on our 2005 Mainship 400. It was not an easy or inexpensive project, my boat was in the yard for almost a month, and I did about 60% of the work myself. If you did not see it, here is a link:
www.trawlerforum.com
The yard manager (good guy, very experienced) and I debated on changing out the starboard tank at the same time. It would have saved a bit of trouble, and a little expense long term, but not as much as you may think. In his considered opinion, the starboard tank had a decent chance to last quite a few years longer and since my budget was stretched to its absolute limit, we decided not to change it. Furthermore, The starboard tank did not leak a single drop the entire time the boat was in the yard.
I agreed with him. We were both wrong.
In what may be the worst luck ever, I got the boat back in the slip, all cleaned up, put back together, running perfectly and less than a month later a hole about the size of a dime opened up in the starboard tank, it leaked so badly that I had to have an emergency pump out done ($$$) and ended up with 3 to 4 inches of fuel in my bilge.
So now I am back in the yard again, the boat is chaos again, the starboard engine is out, the floor is torn up again, deja vu all over again.
This time I decided to cut the tank into pieces and will put a slightly smaller tank back in (I'll lose about 20 gallons from a 156 gallon tank). My generator pulls from the port side, so I don't need as much capacity on the stb tank and cutting saved a little bot of work.
The yard pulled the motor yesterday about 7:30 AM, they found three bad motor mounts. My brother and a buddy came over after that and we worked steady until about 6PM. Got the tank cut and loose in the ER. Pulled up the floor pieces, which were already cut from the last tank removal, and got the tank out today before lunch. Spent 4 hours cleaning after that.
I will post pics as I go along if anybody in interested in seeing the progress.
I'm tired.
Doug
Not sure how many of you followed my thread from April about replacing the leaking port side fuel tank on our 2005 Mainship 400. It was not an easy or inexpensive project, my boat was in the yard for almost a month, and I did about 60% of the work myself. If you did not see it, here is a link:
Mainship 400 Fuel Tank replacement project
OK, this one is not a fun project, not fun at all. Port side tank started leaking in 2018, had an access plate cut in the side and had the tank repaired from the inside, cost about $1,500. It held for 6 1/2 years, so not bad, but it started leaking again in the same spot on the aft bottom a...

The yard manager (good guy, very experienced) and I debated on changing out the starboard tank at the same time. It would have saved a bit of trouble, and a little expense long term, but not as much as you may think. In his considered opinion, the starboard tank had a decent chance to last quite a few years longer and since my budget was stretched to its absolute limit, we decided not to change it. Furthermore, The starboard tank did not leak a single drop the entire time the boat was in the yard.
I agreed with him. We were both wrong.
In what may be the worst luck ever, I got the boat back in the slip, all cleaned up, put back together, running perfectly and less than a month later a hole about the size of a dime opened up in the starboard tank, it leaked so badly that I had to have an emergency pump out done ($$$) and ended up with 3 to 4 inches of fuel in my bilge.
So now I am back in the yard again, the boat is chaos again, the starboard engine is out, the floor is torn up again, deja vu all over again.
This time I decided to cut the tank into pieces and will put a slightly smaller tank back in (I'll lose about 20 gallons from a 156 gallon tank). My generator pulls from the port side, so I don't need as much capacity on the stb tank and cutting saved a little bot of work.
The yard pulled the motor yesterday about 7:30 AM, they found three bad motor mounts. My brother and a buddy came over after that and we worked steady until about 6PM. Got the tank cut and loose in the ER. Pulled up the floor pieces, which were already cut from the last tank removal, and got the tank out today before lunch. Spent 4 hours cleaning after that.
I will post pics as I go along if anybody in interested in seeing the progress.
I'm tired.
Doug