Electric stop on FL80 Diesel

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RobClipper30

Member
Joined
Dec 22, 2020
Messages
13
Hi folks,

Have a problem and thought I’d turn to the collective wisdom of the group for some advice.

New purchase of 40 year old Clipper Flybridge 30ft with the original Ford Lehman 80 HP Diesel.

Electric stop doesn’t work, I can see the arm move a little but it can’t seem to make it all the way so I have to lift the saloon floor and pull it manually each time.

Photo attached. Sorry it’s not great resolution.

Guessing it’s the Solenoid (the white thing?) Battery levels is at full capacity so assuming it’s not power related but haven’t confirmed with voltmeter or anything.

Keen to see if I can fix it myself but have to preface this by saying I’m completely green / novice at all things mechanical but I’m eager to learn if someone can point me in the right direction!
 

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Call Brian at AD. He is very willing to help, and he knows his stuff.
 
Guessing it was originally mechanical, can you rig a line to the lever temporarily until you get someone to look at it?
Is that plastic container the coolant overflow bottle mentioned in the other thread? It`s not the usual kind. If coolant is reducing in the bottle, unless the bottle leaks, it`s likely going back to the header tank which in turn might be returning coolant to the engine. Check for leaks at the cap,usually only 4psi, and anywhere else, esp the tube from under the tank which gets eaten away and loses seal with its hose (well it is/does on a 120).
Where are you in Sydney? I think you need a mechanic. Marinetec on the northern beaches advertise in Afloat Magazine and do Lehman parts, but for now access could be difficult.
A common FL oil leak is the rocker cover gasket, see if it will nip up. Otherwise check for leaks. You don`t tell us the engine hours but some oil use is possible. It does look a tad rusty down there.
 
It's a 40yo engine. That stop solenoid may only need a bit of lubrication inside the bellows protecting the shafts. Dryness may be impeding retraction into the solenoid.

As for the rocker cover possibly being the source of your oil leak, that is a good possibility. I have had that experience. Tightening the securing screws may help but those cork gaskets are certainly very hard now after being in place for many years. Give it a try but DON'T crank down on them too much. If you do, you will certainly bow the mating surface of the cover. If that happens, when you go to replace the gasket you will not get a good seal and may end up with a worse leak. I've been through all of this.
 
My Perkins 4.236 had a manual pull cable shut down instead of a solenoid. Likely a PO replaced a broken solenoid. Cable has always been really stiff and a bit klugey but worked fine. I'm in the process of reverting to solenoid.

American Diesel would be my first call. For me, I needed a bracket that while not cheap from TAD (Perkins dealer, sort of equivalent of AD), was easier than fabricating a bracket. Second, some Perkins injector pumps have integral shut down solenoids - had it been one of those, matching parts exercise would ensue. A plain mechanic would not due.

Good luck

Peter
 
Measure the volts at the solenoid when someone presses the stop button. Those solenoids can draw a lot of amps and the volts can drop too low for reliable action.

Definitely lube the mechanism and check that linkage is not binding in any way.

Also a booster relay can be added so that the high amps does not have to course all the way to the helm and back. Same sort of circuit as used to energize starter bendix. Many engines come from the factory with that relay, some don't.
 
If not to hard to do I'd remove it and take it to a known good battery. Run a couple wires and check it. You eliminate the wiring that way. Doesn't hurt to manually move the cutoff back and forth and a little lube can't hurt either.
If you don't get it to work you have it in hand when ordering another. Either online or in person.
 
Measure the volts at the solenoid when someone presses the stop button. Those solenoids can draw a lot of amps and the volts can drop too low for reliable action.

Definitely lube the mechanism and check that linkage is not binding in any way.

Also a booster relay can be added so that the high amps does not have to course all the way to the helm and back. Same sort of circuit as used to energize starter bendix. Many engines come from the factory with that relay, some don't.


Thanks very much for this - so should I be getting 12v to it?

And what sort of lubricant do you suggest?
 
Due to line losses, I'd figure 10V or below indicates poor wiring. Regarding the lube, anything slimy will work.
 
The solenoid was probably added to replace a cable. If the solenoid is bad, search "12v pull solenoid" on ebay. They run about $10-20.
 
Initially, maybe WD40 or similar,seeing corrosion in the area, then anything,maybe Castrol/Singer Household Oil or similar.
 
IF you have Da Book for your engine you might see a mechanical pull system to stop the engine.

Replace it and your worries will be over.
 
Update

Hey all,

Thanks for the advice. Coming back here with an update after some more tests.

As a recap, pulling the electric stop switch only partially moved the solenoid / arm which wasn’t enough to stop the engine.

Reiterating I’m way out of my depth here but I got the multimeter on it in a few spots per some of the suggestions so please bear with me as I try and explain it.

I’m not sure I had the gauge on the right settings but here’s two photos - first is a reading of 51.6 which is on the bolt/fitting/wire inside the casing attached right to the solenoid. See photo 1 and 2 for examples

Second is further ‘upstream’ on the actual wire that powers the solenoid at 66.2... see photo 3 for example

Both of those only have readings when the stop button being pulled.

Ie I believe I was losing some power in between the fittings and since the pulling the stop was moving the arm slightly just not all the way this is looking to me like a good lead as to the problem?

I thought I’d test this theory and put the positive wire directly into the solenoid so as to rule out all the other little bits. As we pulled the stop cable i got a couple of sparks, the solenoid arm moved all the way (!!!).. and then some safety fuse must have tripped as it turned the ignition off all together.. see photo 4 for example.

So trying to take some initiative I cleaned the connections and even replaced the little ring thing the wire inside the solenoid attaches to (believe it’s called a terminal). See photo 5 for example - I replaced the terminal with a new one and crimped the wire in good and tight.

Put it all back together (loosely not super tight) but now when i pulled sparks flew the first time so I didn’t test it again.

So my main question is do the bolts / terminals / rings / washers etc have some role in moderating the amount of electricity / volts / amps getting from the positive wire through to the solenoid? Or is it that perhaps there is meant to be that much going through but it just needs to be all really tight etc so can’t spark.

Or anything else jumping out at you guys?

Thanks a tonne in advance for any ideas!
 

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set the meter on the twenty it should read 10 or more on the meter . mine needs what ski suggested or tracking down the voltage drop from the top station . but I will have to disconnect the oil pressure alarm can't think with that damn buzzer sounding off . my lower helm works so I know it's wiring the upper helm voltage gage drops like it's in the flybridge feed. does your voltage gage drop when you pull the switch.

also that lever does look strange
 
That bolt with the two washers, where did that attach? Looks strange to me also.
 
Further update

Hi all,

So I got down there today and took a bunch of what I hope are more useful photos and some more multimeter readings.

The first photo I hope shows the setup.

What I did was take this apart and test the powering wire on its own (by which I mean the external wire that feeds from the outside of the solenoid box). It is receiving 11.80v when the stop lever is pulled.

Next I checked the inside wires of the setup ie the terminal inside the solenoid box - 9.10v.

So some power loss happening for sure.

Is this enough to stop the mechanism from working you think?

And what could be the cause? Dirty parts? I cleaned the faces of the little rings / terminals but the bolt was harder to clean.

Photo of terminals and bolt for instance attached.
 

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Last edited:
Clean and lube. Check manually for full action. Clean the electrical connectors.

By the way. Mine stopped working for a while. I didn't have time to troubleshoot it so ran a line (rope) to it and drilled a convenient hole to have it come through the floor. After I found and fixed the problem (electrical) I left the line in place. You never know when you may need it.

pete
 
My FL 120s had a mechanical pull at the lower station to shut them down. Far less complex and so much more dependable that a solenoid. Dump the electrics.
 
If it's loose take it over to the batteries and run a couple short wires to it. Figure out which is the + and -. Connect the - and just touch the +. The solenoid should pop.
That will eliminate or confirm voltage drop being the problem. I'm thinking you should have more than 11 something volts at the solenoid.
If it still doesn't work, replace it.
 
Got on the boat yesterday post fixes and... success!

It was the 40 year old dirty connections after all. Cleaned and replaced and now working great.

Feels so good to have learned a bit about the boat and save a few bucks at the same time.

Really appreciate all the guidance, thanks all!

Rob
 
Hey all,

Wanted to circle back and let you know after cleaning all the parts it’s working! Great feeling having done my first DIY repair to the boat,.

Think I’ll get a physical line put in place for redundancy still as suggested by a few on here.

Thanks a tonne for all the help. Happy boating.
 
Greetings,
Mr. RC. Atta boy! MY electrical "expertise" is average I suppose but my troubleshooting starts with checking/cleaning any and all connections including crimps and grounds. It's also a good time to apply some no-corrode material to the connections and terminals as well.
 

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